Rolling the Die(s)
After a much-needed vacation, I've spent a bit of time working on a prototype host. Progress has been... slow. My biggest issue right now is that the Taig lathe doesn't cut threads.
This is a right pain-in-the-butt because it means I'm using a vise, a button die, and a die stock.
Results have been a little crooked.
I now have a small cluster of brass pills sitting on my dining room table, all of them with crooked threads. Enough is enough! It was time to look at building a proper die holder for the lathe.
I've never machined aluminum on this lathe, and being as a 2" piece was needed, I figured this would be a good project to give it a shot.
The outside cleaned up fairly nicely, though the metal itself was slowly welding to my cutting bits.
It drills pretty wild - huge fuzzy strings of swarf. I'm used to the neat little brass confetti. These big strings had a bad habit of swinging around and slapping my hands with their razor sharp edges.
With the hole drilled through, I switched to the boring bar to widen things out.
The throat of the die holder
should now be only a tiny bit larger than my die.
But the best way to check is to pop the die in there and see how things fit. Success!
The aluminum wasn't all that kind to my machine. I think a larger, more sturdy lathe might be a bit more pleasurable to work it on. There was a lot of chatter/squealing throughout this project - you can see the slight chatter marks on the beveled edges I put around the holes.
I flipped the workpiece around in the jaws, trying my hardest to align it perfectly.
Unfortunately, getting zero run-out is pretty much impossible for me. I hid the intersection of the two surface cuts with a very snazzy looking groove around the bottom.
With the die holder complete for now, I switched focus to the brass rod it would ride on. This rod will be affixed to the tailstock ram and allow the die holder to feed itself down the workpiece.
I tested the holder on the rod frequently, looking for a snug (but not sticky) sliding fit. Got it!
The rod will be screwed onto the tailstock ram, so I drilled and tapped it.
The tailstock ram has a little raised area that requires more clearance, so I bored a little lip inside the bar.
After cleaning the chips out of the hole, it was time to see how things sat.
There was the little matter of making sure the die was actually fixed inside its holder. This requires (at minimum) the careful placement of 2 holes exactly opposite of each other at the right height. I started by checking what kind of grub screws the die stock was using, then purchasing some replacements.
That this worked as well as it did
astounded me. I built a Lego tower of slides, hung it off the back of the saddle, and mounted the die holder in it.
A little bit of ink on the side of the holder allowed me to scratch it with my center drill to locate the very edge.
With the hole positioned, there was nothing left to do but drill!
Why stop drilling there though, when we can keep going? :green:
Not only did that work, no aluminum parts were tossed through my forehead in the process! :tinfoil: Time to tap our new holes.
The second you remove a workpiece from a setup, you'll never get it
exactly the way it was again. Rather than risk a crooked tap, I rotated the die holder and manually tapped the other hole using a little wrench.
Now it was time for a little test fit of the new grub screws.
I drilled and tapped one additional hole at a 90 degree angle to the others to serve as a tommy bar.
In addition to working like a handle, it slides along the bed and prevents the die holder from twisting indefinitely as it cuts.
The only thing left to do was try it out! I quickly whipped up a brass pill to test the die holder out on.
The setup worked nicely!
And it cut some straight threads too!
My challenge now is that the 3-jaw chuck doesn't have the necessary grip to hold onto the smooth brass workpiece as the threads are cut. I didn't get a chance this weekend to test it, but I plan to mill 4 flat sides onto the workpiece like this:
... then chuck the flat surfaces up in the flats of the 4-jaw chuck. That should have much better holding power and allow the die holder to cut threads much further down the piece without slipping. A working prototype is tantalizingly close - I'm hopeful that not too many more weekends of side projects like this are necessary to get there.
Until next time!
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